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Coupe都ok 抵用, $1.14/km
Simon 發表於 2010-5-23 19:43


That was because of your NA setting for last weekend.

In the interest of long term reliability of your engine & turbo, best to keep the boost not higher than 1.0 bar.

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剛上大山試一試個1bar的威力.
發覺原來都好勁, 高轉上得好順, 拖波更快更滑溜.
不過有兩個現象.
1.4000-5000轉時有嗚的一聲.
2.車身傾側大, 車快左, 更凸顯coupe反身較慢.
逢星期日...糕-糕-糕.

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Coupe都ok 抵用, $1.14/km
逢星期日...糕-糕-糕.

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個鐘之前壊壊地, 成日無啦啦reset零.
逢星期日...糕-糕-糕.

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提示: 作者被禁止或刪除 內容自動屏蔽

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我都估到你最後要装返個 cheap cheap 機械式水喉制返上去,你都試用咗成年咁濟,盛惠 ..............

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本帖最後由 Simon 於 2010-5-21 14:14 編輯

Project 繼續.
1.換返個水喉制, current max bar set at 0.7-0.8
2.拆左個冷氣電阻, 似乎粒thermofuse真係斷左
3.省左迫力碟, 無左迫力打腳問題.
4.黑色的噴翻黑色
5. 換埋個鐘.
附件: 您需要登錄才可以下載或查看附件。沒有帳號?註冊
逢星期日...糕-糕-糕.

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Still 0.5bar, looks like the problem is with the EBV.
逢星期日...糕-糕-糕.

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打鐵要趁熱!

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Go! Go! Go!

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checked, found the boost controller has incorrectly connected.
Will try some boost run tomorrow. {: ...
Simon 發表於 2010-5-18 21:49



  家下即刻出去試下啦

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checked, found the boost controller has incorrectly connected.
Will try some boost run tomorrow.
逢星期日...糕-糕-糕.

TOP

That is base boost only, you need to check the (i) boost controller pipe works to the wastegate, if they are well secured and try changing the boost controller threshold to see if there is any effect.  (ii) Also you need to check the inlet pipe works to ensure they are tight, and then (iii) the dump valve for leakage.

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弊, 唔夠bar. 只得0.5.
逢星期日...糕-糕-糕.

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Chairman, wait and see if I can spare a racing seat for you.

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本帖最後由 Simon 於 2010-5-18 08:53 編輯

試左車. 引擎一切正常, 水溫, 油壓, 油溫, 怠速800轉, 定過抬油, 一切好正常.
死氣喉聲唔同左, 不過我都未試踩過3000轉.
感覺是, coupe真係快過MR2好多.
發現的問題是
1.原來成套避震都好軟, 浪浪吓. 行左50000km
2.迫力打腳同快車停唔到, 可能係生銹, 行多少少星期六省吓碟同皮.
3.冷氣風機唔行
4. 好想換收音機, and recaro櫈
逢星期日...糕-糕-糕.

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發覺對尾避震好軟, 唔多正常.
Simon 發表於 2010-5-16 21:30


典解會咁㗎?

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回復 100# Simon

Love iT!!!

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發覺對尾避震好軟, 唔多正常.
逢星期日...糕-糕-糕.

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打左一個鐘腊....好攰. 只係打左個頭. 原來架車好大架.
逢星期日...糕-糕-糕.

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